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Post by henri on Aug 10, 2023 7:19:04 GMT
in at mine for a slipping clutch an a couple of other little jobs ,half a day . IMG_2604 by henri briggs, on Flickr . 1st problem ,its supposed to have a fabbri24 clutch in it, so new plates an springs to hand in we go . it hasnt ,some tinkers switched it out for a polini 2 spring clutch in the past . then theres the oil/fuel leak to trace ,an the cherry on the cake , cush drives shot . so half an hour later its on the bench . IMG_2605 by henri briggs, on Flickr . an another hour later all apart , nip out to get more butane for my torch an cush is apart . IMG_2610 by henri briggs, on Flickr . with the source of leak/leaks found IMG_2606 by henri briggs, on Flickr IMG_2607 by henri briggs, on Flickr . an another leak on the base gasket ,guessing it wasnt re-torqued at 100-150 miles after being built . now the rebuild begins .H
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Post by henri on Aug 13, 2023 8:47:51 GMT
cush drive repaired , so bottom end all back together . IMG_2613 (1) by henri briggs, on Flickr . the clutch its supposed to have ,back in ,an a xl2 clutch cover swapped for the long arm cover it had before . IMG_2614 by henri briggs, on Flickr . an then all buttoned up ,ready to run up in the stand ,just in time for the rain to start ,an outside playtimes cancelled . IMG_2619 by henri briggs, on Flickr . H
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Post by jonnysnatchsniffer on Aug 31, 2023 21:38:06 GMT
I bet is was detonating really bad with all that carbon on half the squishband lol There is no hour job with these fuckers, all I seem to do is fettle
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